So I'm still having trouble with the stang any help would be much appreciated. It started after being parked over the winter. Its been bucking, stalling, hesitating bogging, backfiring while downshifting. Stalling at redlight. Missfiring. And here's what I've fixed to help but nothing. Tps, tfi module, different distributor, new cap and rotor, new wires, new plugs, new fuel filter,I've cleaned the air filter, mass air flow, egr. Please help any ideas ?
U should try to clean it out frist just spray so carb cleaner in it it's alot cheaper to do that then gettin a new one my car keep staling and had a really bad idle I cleaned it out and it ran alot better
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Rockin the 7cyl Cobra clone with 231hp to the wheels
the egr if there is one would be mounted to the back side od intake near the throttlebody. look at my project thread and the silver thing on the throttlebody is the iac
Check the wiring harness connections near the back of the intake (look like salt and pepper shakers). You can try taking them apart and cleaning them with a little pick, then put a little dielectric grease in the connectors. My car was running like shit after the winter and that was part of the problem.
Could be the BAP. sensor . DOes it idle rough ... hesitate when cracking the throttle and or pop when you hit the gas ? A bad bap will cause this . It's the sensor mounted to the fire wall with an electrical connector right behind the intake . These sensors are pretty old by now and don't last forever .
Thanks guys ill check out these ideas you had and ill let you know if they work. But really this thing is driving me crazy lol. PROCESS OF ELIMINATION SUCKS.
hurry up and figure this out mine has been doing the same past couple o' weeks fuel pump is last for me. it will be a week before I do it but i will let you know
Mineral O2....the thing on the firewall is 'MAP' sensor just FYI
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1989 hatch lowered, gt40 svo aluminum headed crate motor, tubular cobra upper...just got it new stuff soon....
hay bro i didnt really have as bad as a problem but my car wouldnt idle it would shake and would missfire under load . it turned out to be a bad spark plug that was brand new . it was leaking spark out but i had a msd wire on it so i couldnt see it. mabey something to loook into if you run outa ideas
Well I just picked up a walbro 255 pump and an accufab fp reg las nite. I paid 175 for both. Ill let everyone know if it fixes my problem or not. I don't think it is the plug though because it was having these problems first. Then I changed plugs wires cap and rotor distributor. Thanks though
No I have not done a balance test. How do I do this or where do I go to have this done
You can do it yourself. It's part of the self-test procedure. It can tell you if a cylinder is misfiring or injector is not working properly. It basically shuts down one cylinder at a time and test various sensors. Really effective test if the issue is with a cylinder and is ignition or fuel related
It's easier with a code reader, but can be done with a paperclip. You basically run the check engine codes and at the end perform the balance test. It's at the end of that link.
Btw, I have this kick ass ford code reader I got for 25. Displays numbers instead of blinking lights. Very easy to use. I use mine all the time to stay on top of things and keep my car running great.
not sure yet johnny. i just picked them up on friday. i havent had time yet to install them. maybe next week sometime if i can get out of work early enough. i was just looking for other ideas on what people might think it could be just so if this doesnt work i know what my next step is.
if the pump doesnt work i might check the tire pressure like bighenault said. or i was told i could check the rear passenger break bulb. or the passenger door handle. or worst case senario replace the drivers coor handle. hopefully i dont have to get into these things. "thanks for the help guys" lol
Hey whats the word on the car?????..changed my pump nothing 255lph...took off the top of the motor apart and was going to check heads...upper intake off i noticed the phlonic(?) 1" spacer was a little wierd and not flat. bolted it to intake without upper on and saw light through it very small amount with light off in the garage...got some smaller stocker valve covers and bolted upper intake directly to lower and problem solved, running great with power back!
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1989 hatch lowered, gt40 svo aluminum headed crate motor, tubular cobra upper...just got it new stuff soon....
well i finally found my problem with the car. it was a vac leak. thanks for the help guys i appreciate it. i fixed alot of things on this car because of this problem but now i dont have to worry about any of these other problems